Success Story: Metal Duct Audit

Project 3 — Duct optimization in a textile production plant

Challenge

A garment plant with 12 solid waste discharge points had recurring blockages in polished stainless steel ducts, causing unscheduled downtime and cost overruns in corrective maintenance.

Approach

Waste flow analysis using CFD modeling, review of original construction budgets, and design of a new duct layout with optimized slopes and strategic inspection points.

Implementation

Replacement of 45 linear meters of piping with 14-gauge polished stainless steel, installation of cleanout gates every 6 meters, and a predictive maintenance program based on differential pressure sensors.

Result

78% reduction in blockage-related downtime, annual savings of $23,500 in corrective maintenance, and an estimated 12-year extension of service life. The client reported a return on investment within 14 months.

Supporting Materials
Approved duct plans (PDF)
Technical audit report
Predictive maintenance certificate
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